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iio: gyro: fxas21002c: Fix missing data update in trigger handler
The fxas21002c_trigger_handler() may fail to acquire sample data because
the runtime PM enters the autosuspend state and sensor can not return
sample data in standby mode..
Resume the sensor before reading the sample data into the buffer within the
trigger handler. After the data is read, place the sensor back into the
autosuspend state.
Fixes: a0701b6263
("iio: gyro: add core driver for fxas21002c")
Signed-off-by: Carlos Song <carlos.song@nxp.com>
Signed-off-by: Frank Li <Frank.Li@nxp.com>
Link: https://patch.msgid.link/20241116152945.4006374-1-Frank.Li@nxp.com
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <Jonathan.Cameron@huawei.com>
This commit is contained in:
parent
aaa90d0751
commit
fa13ac6cdf
1 changed files with 9 additions and 2 deletions
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@ -730,14 +730,21 @@ static irqreturn_t fxas21002c_trigger_handler(int irq, void *p)
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int ret;
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mutex_lock(&data->lock);
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ret = regmap_bulk_read(data->regmap, FXAS21002C_REG_OUT_X_MSB,
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data->buffer, CHANNEL_SCAN_MAX * sizeof(s16));
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ret = fxas21002c_pm_get(data);
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if (ret < 0)
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goto out_unlock;
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ret = regmap_bulk_read(data->regmap, FXAS21002C_REG_OUT_X_MSB,
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data->buffer, CHANNEL_SCAN_MAX * sizeof(s16));
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if (ret < 0)
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goto out_pm_put;
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iio_push_to_buffers_with_timestamp(indio_dev, data->buffer,
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data->timestamp);
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out_pm_put:
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fxas21002c_pm_put(data);
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out_unlock:
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mutex_unlock(&data->lock);
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